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sharif101

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Posts posted by sharif101

  1. Dash 7b engine X-Over TIT 830 c & cut back with FF decrease then again 830 with FF increase and stable.Td controlling check 850 deg anti ice on temp increase to 900 deg & not cut back.G/I,F/I TIT almost 100 deg more then #1 eng.TD cal,co-ordinator potentiometer ck, wiring ck TD valve to TD Amp, Engine relay,all check found good.pls any idea

  2. this engine same problem comes again & again.now when throtle forward to 850 degree that time rpm roll back.td null everything is ok.yellow box test only crossover 790 other range ok. thermocouple,harness,wiring,td controlling ck good.only crossover TIT 10 DEGREE more.co-ordinator check resistance high range.if change cordinator can i get good result.

  3. gtc bleed pressure 42psi.leak check 18 sec.but when any engine start button press at that time bleed press decrease to12 psi.all bleed air valve leak check.pls give any idea

  4. With RPM, TIT, FF, and Torque all low, I would think the problem is in the engine. The propeller's job is to maintain 100% rpm, no matter how much power the engine is putting out. If the propeller were to malfunction by increasing blade angle, the FF would not change noticeably, RPM would decrease, but torque would increase. If the prop were to decrease blade angle, torque would decrease, but RPM would increase until it hit the fuel control fuel governor where fuel flow would finally drop, but RPM would remain high. The problem would have to be in the engine fuel system. It sounds as if the TD System being turned on and off creates a difference, and the engine behaves normally in null, drops off power in auto. I would suspect a bad coordinator or bad wiring in the TD system. You might slowly swap TD system components between engines until the problem moves over to the other engine. I know it sounds silly, but with a strange problem like this, you'd be throwing money at it just changing parts. It may not make sense for a fuel system component to reduce RPM, since that is the propeller's job, but it may be taking so much fuel that the propeller drops down to 25 degrees blade angle and cannot maintain the RPM for the power anymore. Without running the aircraft myself, this is all that makes sense to me with the information provided. The problem cannot be caused by an air leak because the drop in torque would be accompanied by an increase in TIT.

    TD valve swap with #1 problem solved but problem did not shift

    THANKS TO EVERYBODY

  5. Hey Bill, I'm with you. Engine or prop change recently? If not, then I'd go with Lkuest. Do a TD check with a test box. Even with a eng/prop change, I'd probably check the TD system on both engines just to be sure and eliminate that.

    Not being an engine or prop guy, have you given any consideration to the fuel control or prop governor? Maybe blade angle on the prop?

    I'd be curious as to what all 4 are doing. Compare 2 & 3 to 1 & 4 with them all running. At NGI it appears that #2 is higher than #3 so I might think fuel control at first.

    Not bad for an OLD 32nd guy huh Bill?

    engine & propeller change few days ago.when rpm decrease at that time FF,TIT,TRQ rapidly decrease.td test found set,blade angle ok.

  6. dash 7b engine #2 eng LSGI TIT 700,FF 600.#3 eng TIT 700,FF 650.normal GI #2 eng TIT 700, FF 950.#3 eng TIT 600,FF 800.

    x over #2 eng TIT 800 FF 1500 in auto, FF 1700 in null.during take off RPM 100%,FF 1950,TIT 977 then decrease to 97% and stable in TD auto with mech gov & normal but TD null RPM 101% with mech gov & normal no change.now what can i do?please help.

  7. yes, i checked coordinator both 65&66 degree switch.relay box replace new one.now problem shifted today given ground run 2 times.TD null 3times check but 1 time flame out.last time when TD auto and throtle back to flight idle TIT 720 degree then flame out with sound at that time FF increase 500pph,TIT above 900 degree & RPM 93%.i think bleed valve open since RPM below 93%.is it FCU problem?ssv filter check ok.pitch lock regulator replace new one.Xover TIT 775 degree.

    can i change acceleration bleed valve?

  8. all throttle position FF,TIT,RPM,TRQ normal but only throttle back to just below Xover then flame out & sound produced 2-3 second interval but when TD null then no flame out.TD ams test check 2 times found good,cordinator check ok,thermocuple,harness,5th & 10th stage bleed valve,turbine check found good.now what can i do?pls anybody help

  9. on dash 7b engine #3 engine propeller brake locked then we try to unlock but failed.we gave apprx 10 us gal hot oil inside the RGB for prop brake release but failed to release.then RGB change & engine fitted.during Ground run found oil flashing from bleed valve ,drain mast also white smoke from tailpipe.we attempt 2nd start found no white smoke but during power reduce from takeoff to below x-over at that time flame out with poping sound after 2-3 second interval it happen several time at that time i shutdown engine manually.during flame out fuel flow increase suddenly.other parameters normal.TD sys calibrate & TD valve changed again ground run but problem remain

  10. GOOD MORNING EVERYBODY

    When all four engine low speed at that time ATM did not haullt.engine low speed bleed pressure is 28.bleed air no leaking.even GTC (40psi) pressure did not hault ATM.replace new ATM but problem still.

    pls give idea

    THANKS

  11. GTC bleed pressure 42psi.leak check (30-15) 7.5sec.i changed flow control shutoff valve,cargo,flight deck shutoff valve,ATM shutoff valve,both wing isolation valve,Empannage anti icing & pressurr gage.Check all anti iceing vale,starter control valve,wing bleed valve,eng check valve.cargo comparment all duck checked.no leak found but problem not overcome.previous leak checked founf 12 sec.

    please give idea

  12. without eng(-7b) start.if #1 throtle foward above 65deg fuel correction light goes out.other eng correction light not goes out.#1eng parrameter ok.s.s.control change,cordinator ck good,throtle rigging,td amp check.what may be caused.

  13. So, if you are checking this during an engine run, with all four engines on speed, the #3 pump fails with all 4 generators online? Does the pump start working when you switch the #3 generator switch off?

    You don't have any AC bus off indications?

    dear,now problem was changed which is #3 generator voltage, frequency normal but dont load to operate boost pump,aux pump .ac bus off indication ok.generator new.

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